I was not being clear. So on the previous tune, it was knocking really really bad, Koji was able to fix most of that. Koji's dyno read 15% lower than the previous tuner's dyno, making my final # same as previous tune.
9:1 theoretically should make more power but for whatever reason, it started knocking as soon as boost started settling in. Before setting up a dyno time, Koji explained that from his previous experience, 9:1 usually knocks bad and stated that my set up will not make more than 280 @ the wheel.
I'm guessing the previous tuner pulled timing to avoid knock, which caused my egt to get so high.
I've sourced most of the parts which involves dropping CR to 8.5:1 (head gasket) along with bigger/better injectors, pumps, and intake. I'm planning on doing these after the 4/1 event and go back to Koji.
I really appreciate your concern! Feel free to comment on whatever!
I have not done much of that which I need to do eventually. NO AC, gutted interior/ sound deadening, lighter battery, titanium exhaust is about all I have so far. Car weighs around 2600lbs with full cage which is not bad..
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I've also added a separate relay that powers the fuel pump.